Pond V3: Chapter 1

The backyard pond is getting a major, final (hopefully!) upgrade this spring. The past 2 years have been a learning experience. I believe I’m ready to put the finishing touches on it now. Those “touches” as t’were, entail a complete overhaul. One issue is the goldfish. They are getting BIG! Here’s a pic of them in their 125gal basement winter tank:

Goldfish01
Another thing is/was that plastic fountain I put up last year. It looked OK and everybody seemed to like it, but it just started feeling a bit cheesy to me. After some thought I came up with an idea for a permanent, more natural and elegant-looking fountain. It will tie into a concrete surround slab raising the water level about 6 inches this time. The sump seal is being re-designed and I’m going to replace the liner and dig it deeper. Goals for the work will be zero seepage and a significant capacity increase Here’s what it’s looking like after a good start over the past couple of weeks:

Pond Start

Junipers Out, Roses In

The very first flora we planted right after moving in back in 2003 was 3 Junipers outside Phoebe’s bedroom window:

Junipers
I viewed them as a security measure more than anything else, blocking access to the window and basement egress. We had an early hard freeze in 2013, that pretty much killed them. I say “pretty much” because they did survive just barely, but remained mostly brown for the next 3 years. I hoped they would eventually fully recover, but it wasn’t happening.

I started a somewhat related project in the spring of 2014 to install a sump in the egress window well. We’d always been getting water in there for some reason, I assumed just because the soil here is sandy and drains really well. So I did a little digging on-and-off over the next 2 years, not really in any hurry. Little did I know, the Juniper project would finally reveal exactly why water was going in there and rusting the window well shell.

The problem became quite clear after pulling the Juniper stumps. Some fool builder decided to back-fill around the window with landscape rock! Not completely, but enough to make a negative grade down almost 2 feet on 1 side. So I had to dig out about 500lbs. of rock and properly back-fill the thing with soil. Despite not really needing it anymore, the sump project finally got completed in conjunction with a new flower bed containing 2 rose bushes for starters.


The window well is still not actually quite complete. It needs a cover, which is going to be another custom DIY. I also have to get around to cleaning up and painting over that rust one of these days as well…

Old-Fashioned Gauge in a New-Fangled Car

The low pressure side of the commonrail fuel system often gets overlooked, but plays a crucial role. I was pleased to see BMW specs nominal CP3 input pressure at ~5 bar. They probably used a fairly good quality lift pump in the tank which will likely never need replaced, assuming you ascribe to the fuel lubricity additive concept. Fuel supply flow capacity needs to increase proprtionally with power-adding mods. That does not appear to be an issue with this setup. My lift pump holds a rock-steady 60psi with the go pedal matted and JBD at 100%. But there are other things to consider. Cold weather for example, induces fuel viscosity increase, severely reducing pumpability once temps drop near zero and below. That’s why we have a fuel heater, but it can only do so much. Anything constraining fuel supply flow can quickly lead to injection pump damage. Unfortunately there’s no shortage of different ways to get things FUBAR’d on the upstream side of the CP3: cold weather, bad fuel (water especially), filter degradation, various lift pump malfunctions, etc.

The failure mode varies, but sudden catastrophic loss of the CP3 can take out everything in it’s path. Many parts are subject to damage, potentially requiring replacement of injectors, sensors, and at a minimum, a complete fuel system flush from head to tank. Dealers confronted with it often elect to simply replace the entire fuel system. It means lots of parts and labor hours, but ironically, ends up being quicker and easier in the long run if one thing after another starts turning up bad during a piecemeal approach. But this is all easily avoidable with a little monitoring. I understand the car’s sensors and software will set codes for a plethora of fueling paramter anomalies. But I doubt it’s ability to forewarn impending problems or long-term degraded conditions in the fuel supply like a simple, mechanical guage.

There are a couple of fairly serious issues involved with using a mechanical fuel gauge in the cabin. There’s a small chance it will fail in some way as to allow a leak. A worst case scenario might be something like it explodes spraying fuel in your face while driving in heavy traffic smoking a cigarette. My customized combination shutoff valve/snubber mitigates this issue and another problem fairly well. The other problem is CP3-generated pressure wave reflections wreaking havoc with the gauge readout. Installing a ball-bearing poppet in the valve’s gauge port stifles that phenomenon. The rubber valve seal gets soaked in gear oil while doing up the valve assembly to induce swelling to the point of actually making the thumbscrew harder to turn after reassembly. Done right and reassembled using JB Weld for thread locker, the valve will never leak and just cracked open provides a safe, stable analog/mechanical fuel pressure reference to the gauge.

Exploded Valve
Mounted Valve
Tapping the fuel line post-filter is not exactly straightforward. There are lots of candidates for places to do that, but BMW’s proprietary faux plastic lines and fittings everywhere take all the fun out of it. A good way I found was to slide the stock filter back a couple inches in the mounting clamp and clock it about 15 degrees. This creates enough room to splice in the adapter quite nicely. Remember you are working on the clean side of the filter, so parts and activity related to opening it downstream of the filter must be meticulously maintained in pristine cleanliness. If not, the car will immediately tell you about your failure to do so upon restart.

Gauge TapA
Gauge TapB
Gauge TapC
I expect fuel filter maintenance intervals to increase significantly with the ability to actively monitor fuel pressure. Filters filter better the longer they are in service, right up to the point where they can no longer meet the flow requirement. I believe changing filters of almost any type on a schedule is just dumb. Of course there are specific exceptions to the rule, but they are limited to special types of equipment and conditions not in the consumer automotive realm.

Dumpsters behind quick lube joints across the country are always full of perfectly good filters. Also, it should be interesting to see pressure fluctuation (or not?) with a hotter tune at some point. I have a feeling fuel supply is not going to be an issue. The 9mm ID tubing should be adequate for up to around 400hp.

Instrument Panel

Spring Blizzard!

Last week’s snowstorm was nice. I mean, really – we needed the moisture. Looks like we’ll get double that amount or more today, and the wind is howling. It’s a full-blown (and I do mean blown) Rocky Mountain spring blizzard!

NWS Report
Doppler Radar Map

Spring Snowstorm!

We have 7″ after 24hours of pretty much continuous snowfall. Some places got more, others less. Should be over by this afternoon and gone by Sunday. Does make for an interesting Friday morning commute though, no doubt. The only roads not jammed are around the airport, and that’s probably only because alot of flights are cancelled.

Spring Snowstorm

Francie's Off to Orlando

Francie left for the airport with Avery about an hour ago. This is the big Volleyball Club trip she’s been looking forward to. Hopefully they will do well in the tournament and she’ll have plenty of new stats and video to impress the college recruiters with. It’s also her first trip away from home more-or-less on her own. They do grow up fast.

Francie V-Ball

UI Claim Official – "Exhausted"

Paul D. Shaffer Status Update: Retired! And that’s OK by me, because I really am “exhausted.” Apparently my unemployment benefit ran out. At least I haven’t heard about any extension. So if the government no longer considers me “unemployed,” I guess that means I must be “retired,” right? Excellent.

Fish Babies!

The Convicts spawned again. Last time was almost two years ago in the old tank. I guess they finally became comfortable enough in their new environment to go for it. Should be more interesting watching the fry grow this time around. Mom and Dad are quite busy keeping predators at bay and digging them out of the gravel when they get stuck. Pretty cool stuff:

Convict Babies

Phoebe's Off the Payroll

Well, not exactly – she still lives here. But she is working for Bed Bath & Beyond, for going on 2 months now. Her first job about a year ago was part-time for Mc’Donalds and lasted all of three weeks.

Feeb

Latest Frankenputer

The basement workstation started getting more flakey than usual by repeatedly refusing to POST, hanging at the EMT64 message. It’s done this on and off once or twice at a time almost since new 12 years ago. I attributed it to some quirk of the Asus MB, but despite otherwise running flawlessly all this time, it seems whatever is causing that issue is getting worse. Rather than fix a PC that is one of the newer boxes and technically still “working,” I decided to upgrade the oldest one sitting next to it. The object was to have a more reliable, man-cave workstation while getting rid of a basically obsolete system at the same time. The only parts I needed to buy were the MB, RAM, CPU AND a DVD burner I got from Newegg for the Low-Low price of $15. Total cost for the project right around $400. I re-used an old Mylex raid card and drives from the parts bin because I recently learned 60Gb (size of the SSD’s also from the parts bin, being transplanted into it) is no longer enough for a Linux PC with all the stuff I like to have on it. It’s now a beefy, fully redundant high-availability system.

Specs:
ASRock Z97 Extreme3
Core i5, 3.5GHtz
16Gb DDR3 Dual-Channel RAM
2x Corsair 60Gb SSD (Primary sys drive w/hot spare)
2x Quantum U160 74Gb (/var/home/tmp on Mylex Raid1)
3x WD Blue 1Tb (2Tb MDADM Raid5 data volume)

asrOCK1
asrOCK2

335D Still Getting Better

The w/m injection nozzle coupling worked it’s way loose somehow. I discovered it after dumping about 3 gallons of juice on the road between the time that started and when I identified the problem. So while I was at it I decided to upgrade it to a 2-stage system. The trucks use progressive controllers to modulate delivery, but I really doubt the efficacy of those devices in normal use. The main purpose for having it on the “D” is keeping the intake clean. It can also add a little power. I theorized a more practical approach would be two injection events, a smaller nozzle coming on earlier more often, and a bigger nozzle coming in only at or near full load.

1st phase of the project was installing a 2nd smaller injector, size M2. The original M3 stays put in the intercooler coupler, after of course modifying the connection to keep it secure. I suppose those push-in 1/4″ pipe couplers are OK, because I never had this problem until now, after years of using them on the trucks and continuing to use them at various locations in this system as well. A hose barb reinforced with JB Weld is not coming apart without a forcefully applied tool. Here’s the new nozzle mounted right at the manifold flange:

Nozzle
Nozzle2
Phase 2 involved setting up a solenoid valve to fire the original M3 injector off a secondary pressure switch set for the max boost range starting ~24psi. I began by testing with the spare pump to ensure it would effectively atomize 2 injectors, because it’s a pretty small pump. No worries there. Setting the boost switches accurately was a frustrating moving target at first. The engine will see somewhere around a 3psi delta on the high side parameter depending on a number of factors. 22psi is where it typically tops out, but I’ve seen it pull 25 briefly under heavy load.

I used 1-amp fuses on the pump and solenoid circuits to dial it in pretty close to my target settings. Those switches from McMaster Carr are quite sensitive and accurate. I started with them set high and repeatedly ran the car to the desired boost setting, stopped and checked the fuse until it blew. Took three tries on the high switch and about 6 or 7 on the low switch. I haven’t run it with a boost gauge installed since removing Burger’s JBD tuner last summer, but I imagine it should go higher with that extra fuel.

After a couple weeks of using too much water while randomly fiddling with the switch settings I ended up making a tool for pressurizing the system manually to see exactly where the switches were tripping. It probably would be better to tap into the MAF sensor for this purpose, but I’m still a little skittish about the electronics on this high-tech Teutonic contraption.

The pump supply line tees off to the primary injector before the secondary solenoid valve:

Solenoid
The last phase was simply getting everything wired up, plumbed and tested: Pressure Switches:

Switches
The air, or “boost side” of the system literally comes together on the driver’s side shock tower. Both switches and the gauge reference the same charge pipe feed at this junction:

Junction
The car has a Boost Gauge mounted in the instrument cluster. It’s more of a testing tool that anything else, necessary to fine tune the pressure switches. I used the high-pressure gauge on my compressor to set the switch before, but it’s not good enough at lower pressure to see the 1-psi increments needed for this application with any accuracy.

Compared to the single-nozzle version which came on at 20psi, the system now provides >60% more water/meth on the top end, while delivering about 30% less at moderate load between 18 and 24psi boost. I expect the real-life consumption rate to go up spraying less more often, based on my driving habits. Before I was using about about 1gal/tank of fuel, really only hitting it with go pedal down hard. I’m hoping this new setup equates to better cleaning in normal driving.

Dash1

Solar Power!

We finished the system install last Friday, including inspection by the local authority. Now just waiting for United Power to come and install the meter. Before:

Before Solar
After:
Solar After
I really like how it is arranged to avoid the neighbor’s house shadow. We went with a local company out of Boulder, Namaste Solar. I had an aborted attempt a couple of years ago with a larger nationwide group called Solar City. I was unimpressed with their customer service, as is sadly, typical with larger companies. But Namaste did a great job and I would highly recommend them to anybody looking at a Solar project in the area.

Not Too Shabby, Methinks

$75/mo, w/basic cable:

Speedtest.net

The cool thing about this is we got a no-cost bandwidth and cable box upgrade. We had no cable TV before I called to activate a new modem the other day. It’s a newer 16 channel TP-LINK Archer capable of supporting higher speeds. For some reason, the woman I spoke with in the Philippines offered an upgrade – gratis. The cable box showed up a few days later. It was obviously the standard bait and switch with a limited basic cable package we’ll probably never use. But the Internet speed is great and I have to give them credit for getting their crap into my house after I swore long ago to never again succumb to the cable TV ripoff scam. Kudos Xfinity!

Best Bridge in Raleigh

Well, of course that’s debatable, but considering old-school craftsmanship and skill, undoubtedly true!

Joe's Raleigh Bridgework
Joe spent _ years completing this project for a customer’s backyard in Raleigh, NC. VERY nice work, dont’cha think?

More Pics

Right Shoulder is Done

Now with Video! The video portrays just one of three separate operations performed. He also repaired a torn rotator cuff and and removed several bone spurs.
There’s another hole in back – 4 incisions total:

Shoulder Arthroscopy
It was a mess in there. He also had to cut the subpectoral biceps tendon – too far gone to repair.

Waikiki, Baby!

…it’s freakin’ awesome. Honolulu is too crowded and the traffic is horrible. But no complaints other than that. Hotel is amazing – even nicer than what I’d heard. I’m sitting at the beach bar sipping a diet Pepsi while Phoebe irradiates herself. Michelle and Francie are somewhere on the other side of Pearl swimming with dolphins. Nice:

waikiki beach
waikiki beach
We have a buttload of pics I’ll be processing into the Photo Album, as time permits.